Alright, so I had a chance to run through some things.
Pulled off the bowl, pilot jet, air mixture screw, and blew carb cleaner through it all. Everything seemed clean, some small rubber pieces from the air filter have been coming off from taking them on and off so i was hopeful that a piece got stuck in a passage.
Didn't see anything though.
Started well, idled well, the exhaust was a little black, but when i held a white rag at the end of the pipes, it didn't discolor it badly...if that means anything. I was going to pull the plugs after 10 minutes of idling only and take a look, but being it was idling smoothly, and I forgot the choke on for the first two minutes

, and I'm sure sooted the plugs, I gave it a bit of throttle, and that's where it stuttered.
So pilot jet is #15, throttle slide is 2.0, needle jet is Q2, jet needle is 6F4 leanest clip, and main is 145. I haven't pulled out the air screw that's in the bellmouth, typically they're a 2.0 so I'm assuming that's what it is, pretty good sized hole. I wonder if I pull it out completely and see what effect I get??
So checking in with the pros, would you change out the throttle slide next to a 3.0 or 2.5, change the needle jet to a P5 or so, or order them both up but change only one thing at a time? Any other ideas, I think I'm going to take out the air screw to see what affect it has? Thanks